|Subject:||Re: [Paparazzi-devel] Critical behaviour of baro_ms5611_i2c|
|Date:||Mon, 28 Jul 2014 23:14:21 +0200|
the reason for I keep post here is because I still don't feel confidence
with this problem and solution. and I found some strange behave of my UAV.
here is the log.
I don't go into the code to see the estimator handler, but I guess it is
joined with GPS alt with baro estimation, right? GPS alt look reasonable,
so the only problem could be baro output, still have some abnormal peak. I
have to check it again.
I will keep you in post.
View this message in context: http://lists.paparazziuav.org/Critical-behaviour-of-baro-ms5611-i2c-tp11592p15933.html
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